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30th January 2020, 19:20 | #1 |
I really should get out more.......
mg 190+ Join Date: Feb 2013
Location: Bedworth
Posts: 2,267
Thanks: 191
Thanked 368 Times in 248 Posts
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Waste of a day
Went to look at 2 Conn se v6 today.
First one looked great in brg Header tank cap was very tight . So had to get them to take off. Started ok but had a knock from around the belts area. Let it run a bit.and yes sure enough started pushing water out the top with a nice mix of air. But the cap back on and it still pushed coolant out. Sales man insisted on putting the cap back on and tighting the cap to breaking point. 2nd one looked nice in black. And that's as far as it went. Boot so full of water that it covers the tyre. Intake was so loud that it was loads louder than the engine on tick over. Then the code reader went on. Gearbox ECU fault Injector fault Misfire Fan not working Sales man says it's ok we will sort it all out and replace it all that's faulty. I just said good luck when you see the price of the inlet manifold So 300 miles and not even a sniff of a good 75 connsuer se |
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